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Over pressurised piping causes line failure

What happened - icon

What happened?

A coiled tubing crew was conducting pressure tests of the blowout preventer.

Following a successful low pressure test at 10 Megapascals (MPa) the line was bled down through two-inch diameter blowback piping to an open-top tank. This pressure was bled off without issue, confirming that the line was free of obstructions.

At this time, a  high-pressure test was conducted at 55 MPa. When the valve was feathered open to bleed off the pressure, a loud bang was heard, and the piping parted.

Several workers were in the vicinity of the flying debris, but nobody was injured.

View of blowback piping and tank on the north side of site prior to overpressure event.
What happened - icon

Why did it happen?

The blowback piping was over pressurized.

It was rated for 14 MPa and because it was vented to atmosphere, it was believed that the risk of an overpressure event was low.

View of where blowback piping (circle) and fitting (arrow and star) landed on south side of site.
What happened - icon

What did they learn?

  • The blow-down procedure was modified to step down the pressure from the high-pressure test before going to the blowback piping.
  • A pressure transducer was installed on the blowback piping to monitor the line pressure. This has since indicated that overpressure events were likely occurring frequently.
  • A pressure safety  valve was installed on the blowback piping.
  • Piping restraints were added to the blowback lines.
  • Equipment layout was modified to shield the manifold operator from the blowback piping.
What happened - icon

Ask yourself or your crew

  • How can something like this happen here (e.g. on our site)?
  • What safety measures (i.e. procedures, controls/barriers) do we have in place to mitigate the risk?
  • How do we know the risk controls/barriers are working?
  • What improvements or changes should we make to the procedures, controls/barriers or the way we work?
  • What happened?

    A coiled tubing crew was conducting pressure tests of the blowout preventer.

    Following a successful low pressure test at 10 Megapascals (MPa) the line was bled down through two-inch diameter blowback piping to an open-top tank. This pressure was bled off without issue, confirming that the line was free of obstructions.

    At this time, a  high-pressure test was conducted at 55 MPa. When the valve was feathered open to bleed off the pressure, a loud bang was heard, and the piping parted.

    Several workers were in the vicinity of the flying debris, but nobody was injured.

    View of blowback piping and tank on the north side of site prior to overpressure event.
  • Why did it happen?

    The blowback piping was over pressurized.

    It was rated for 14 MPa and because it was vented to atmosphere, it was believed that the risk of an overpressure event was low.

    View of where blowback piping (circle) and fitting (arrow and star) landed on south side of site.
  • What did they learn?

    • The blow-down procedure was modified to step down the pressure from the high-pressure test before going to the blowback piping.
    • A pressure transducer was installed on the blowback piping to monitor the line pressure. This has since indicated that overpressure events were likely occurring frequently.
    • A pressure safety  valve was installed on the blowback piping.
    • Piping restraints were added to the blowback lines.
    • Equipment layout was modified to shield the manifold operator from the blowback piping.
    What learn - icon
  • Ask yourself or your crew

    • How can something like this happen here (e.g. on our site)?
    • What safety measures (i.e. procedures, controls/barriers) do we have in place to mitigate the risk?
    • How do we know the risk controls/barriers are working?
    • What improvements or changes should we make to the procedures, controls/barriers or the way we work?
    Ask your crew - icon
Published on 05/04/23 1100 Views

A coiled tubing crew was conducting pressure tests of the blowout preventer. Following a successful low-pressure test, the line was bled down through blowback piping and a high-pressure test was conducted. When the valve was feathered open to bleed off the pressure, a loud bang was heard, and the piping parted. Several workers were in the vicinity of the flying debris, but nobody was injured.